plans called for three layers of 2oz fibreglass to be laid up inside the hull but I went way above this specification, trying to build more strength into the boat. As bulkheads were fitted and glassed into position we started to use new terminology: we would be working in the forward compartment, the heads, or main cabin.
After completion the decks would be lowered into position with a 2in lip running around the outer edge until it came flush with the top of the hull. It was then through-bolted, and later capped with wood to make the toe rail. The inside corner would be glassed-in to give more strength and make it watertight.
Brian asked for layers of fibreglass to be left out as he wanted a lighter, faster yacht, but he put strength back by running two Iroka beams along each side of the boat, under the deck, which were then glassed in position. He also put a third beam across the rear cabin bulkhead. Through-deck U-bolts took the standing rigging.
I followed Brianâs example despite the fact that I had been adding weight instead of reducing it. By this time people were saying I was over-building
Solitaire
, using backup systems to back up systems but I knew she would have to look after both of us until I could learn the ways of the sea and sailing.
If you asked the driftwood what they remembered about me, they would probably reply, âLeslie? Oh yes, he was the one who cut a blooming great hole in the bottom of his boat.â In fact it was 9in wide and 4ft long. I had never liked the skeg, which was hollow, and, when banged with a fist, would vibrate. I spent a weekend in Tony Marshallâs garage building a replacement of Iroka, a modification which one day was to save
Solitaire
â andme. The size was increased to allow 10in to extend into the hull for bracing with a hole drilled ready to take the stern tube and propeller shaft.
For a few days the boat sat with a gaping hole in her bottom. To lifted eyebrows and inquiring looks, I would merely say, âMice.â
In June my mother was taken to hospital which meant that I had to return home. I managed to find a good position with Ken Mudd as a quality assurance engineer for British Leyland.
Solitaire
was moved 80 miles overland into a field where I fitted her out, buying unplaned planks of Iroka for her interior. Most of the work was carried out with the help of an old friend, Tony Marshall, who had started out as a carpenter. Len Westwood, a foreman motor mechanic at British Leyland, helped to fit a new 18hp Saab diesel engine.
When the time came to install
Solitaire
âs ballast, I bought 2 tons of scrap lead but could not decide how to pour the casting. I considered using an old bath as a melting pot, but the snag was manoeuvring this lump into the boat now that her deck had been fitted. When in doubt I did what I always did â phoned Brian Gibbons. He had got over this problem by building an adjustable die with which you could make ingots to suit the shape of the keel. Having borrowed it I spent two days in Tony Marshallâs back garden where we cut a 32lb gas bottle in half for use as a cauldron. For heat we used coke with a couple of car air blowers. The resultant 80 castings fitted to perfection and with a few gallons of encapsulating resin the job was completed.
Solitaire
began to show her beauty and was ready to be christened in seawater. A government agent had visited and presented her with a British birth certificate. She was painted and antifouled; mast, boom and rigging ready for fitting.
Although Rome had been stationed up north we kept in contact with weekly letters and the odd visit. He already had a berth in Lymington, his home town on the south coast. In March 1975 he took his yacht there, so I went along to lend a hand and to learn the ropes. There I was introduced to his mother, Grace, a fittingname for such a lady with her easy smile and quick laugh. Born in South Africa, she still had tinges of the accent. I met her